19-Aug-2023 | |  | Nose wheel flat, inner tube needs replacement. Will pick up part on Monday. | Andreas Casal |
21-Aug-2023 |  | | Nose Wheel inner tube and tire replaced. | Maintenance |
21-Aug-2023 |  | | 50 Hour Inspection Carried Out. | Maintenance |
16-Oct-2023 |  | | Right fuel cap rubber seal and teflon slip ring replaced after it was suspect in fuel mysteriously dropping faster in the right tank when flying. | Maintenance |
29-Oct-2023 |  | | Could not get fuel to flow out of the supply tank after the flight on Wednesday. Chris Meelker suspects it might be a worn seal and will investigate. | Hal Sabeti-mehr |
30-Oct-2023 |  | | Fuel pump shaft o-ring replaced, pump spins freely and does not leak. Tank is at ~150 gallons. Was able to prime the pump by placing the fuel hose on the ground, after which it pumped freely. | Chris Meelker |
22-Nov-2023 |  | | ELT removed for recertification. | Maintenance |
26-Nov-2023 |  | | ELT installed after recertification at Hi-Tech Avionics. | Maintenance |
27-Nov-2023 |  | | ELT installed after recertification at Hi-Tech Avionics. | |
27-Nov-2023 | |  | Propeller removed and sent to Hope Aero for 5 year corrosion inspection | Maintenance |
4-Dec-2023 | |  | The current aircraft lease has expired and the new one is not yet signed, making the C of R invalid. This should be sorted shortly but at present the aircraft is not legal to fly. | Chris Meelker |
8-Dec-2023 | |  | The new lease has been signed and the Interim C of R activated while TC processes the paperwork. Aircraft is good to go once maintenance is complete. | Chris Meelker |
19-Jan-2024 |  | | Propeller installed after 5 year corrosion inspection at Hope Aero. I do apologize for not posting this earlier as the web site was down for a while. | Maintenance |
2-Feb-2024 |  | | 100 Hour Annual Maintenance Completed - Serviceable | Maintenance |
21-Feb-2024 |  | | Tanks are almost 1/2 full. Unable to produce any flow from pump. Recommend planning a fuel stop at an alternate airport. | Hal Sabeti-mehr |
4-Mar-2024 |  | | During the flight thr Push to talk button on LHS got stuck several times. | Debra Teelucksingh |
4-Mar-2024 |  | | Pump unable to produce flow. Filled up tanks in Brampton . | Debra Teelucksingh |
6-Apr-2024 |  | | Note from parking neighbor: Please be advised that there are a lot of starlings at his airport in spring looking for places to nest. Cover any openings if possible. CFYLH | Andreas Casal |
5-May-2024 |  | | Worked with Alan on the phone to troubleshoot over-voltage light staying on. Issue resolved. Bird droppings on H-stab, elevator, and fin cleaned up with non-alcoholic baby wipes. Alan advised not to use isopropyl alcohol baby wipes | Hal Sabeti-mehr |
6-May-2024 |  | | Note: recent rains have made movement around / through existing potholes in pavement difficult. Will contact BFC to see if they can get those areas repaired. | Hal Sabeti-mehr |
12-May-2024 |  | | Insurance documents updated | Andreas Casal |
31-May-2024 |  | | Drain valve (CCA2800) leaking. Replaced by brampton maintenance (Aaron). Journey log entry by mechanic | Peter Barbuto |
30-Jun-2024 |  | | Grass around RAJ cut and trimmed Thursday evening June 27, 2024. I brought along a weed/grass trimmer as the grass was up to 12 inches (I don't think the push lawnmower would be able to get through it). | Maintenance |
9-Aug-2024 |  | | Aircraft Status logs are operational again. | Graham Elliott |
9-Aug-2024 |  | | 50 Hour Inspection carried out. Compass Swing carried out. Grass surrounding airplane cut and trimmed (it looks nice again). The Mode C Transponder Correlation Recertification will be done by the Brampton Flying Club Maintenance on Thursday, September 5th at 9:00 a.m. (usually takes an hour or so to do). | Maintenance |
19-Aug-2024 | |  | Nose wheel found flat while connecting tach sheets. Added air but there is an obvious leak between the wheel halves. BFC maintenance will address during the week. [19-Aug-2024: Edited by C.Meelker] | Chris Meelker |
22-Aug-2024 |  | | Nosewheel tube replaced by BFC maintenance. | Chris Meelker |
17-Sep-2024 |  | | Main landing gear left and right tires replaced with new tires and grass around airplane trimmed/mowed a week or so ago. | Maintenance |
17-Sep-2024 |  | | Altimeter replaced and cracked static port replaced, followed by Mode C Correlation Recertification by BFC Maintenance. | Maintenance |
16-Nov-2024 |  | | At start up after confirming the altimeter setting to Brampton’s weather report of 30.11”hg the readout was 836 feet compared to 936 feet (field elevation) under reading by 100 feet | Peter Barbuto |
3-Dec-2024 |  | | Good News: Airplane was taken into BFC Maintenance for altimeter issue. BFC's resolution response: I verified your snag and found that the altimeter was 90’ off from the calibration card supplied with the unit. I recalibrated the altimeter and verified the accuracy up to 20000’. It is now within limits. | Maintenance |
1-Feb-2025 | |  | Annual Inspection Due | Maintenance |
25-Mar-2025 |  | | Annual Inspection carried out. It's good to fly (but the log book is currently with me - Alan). | Maintenance |